Trans International Airlines Flight 863


Trans International Airlines Flight 863 was a ferry flight from John F. Kennedy International Airport in New York City to Washington Dulles International Airport. On September 8, 1970, the Douglas DC-8 crashed during take-off from JFK's runway 13R. None of the 11 occupants, who were all crew members, survived.

Aircraft and crew

The aircraft involved was a Douglas DC-8-63CF, that was built in 1968. The aircraft was powered by four Pratt and Whitney JT3D-7 engines. The aircraft had 7,878 hours and five minutes at the time of the accident.
The captain was 49-year-old Joseph John May, who had 22,300 flight hours, including 7,100 hours on the DC-8. Other TIA pilots referred to him as "Ron". The first officer was 47-year-old John Donald Loeffler, who had 15,775 flight hours, with 4,750 of them on the DC-8. The flight engineer was 42-year-old Donald Kenneth Neely, who had 10,000 flight hours, including 3,500 hours on the DC-8. There were also eight flight attendants on board.

Accident

At 16:04, the aircraft was cleared to take off from JFK Airport runway 13R. The take-off roll commenced one minute later, at 16:05. The takeoff was unusually slow, with rotation occurring down the runway. Due to the slow rotation, a tailstrike occurred and skidded on the runway for. The Cockpit Voice Recorder recorded the sound of the tailstrike.
At 16:05:35, captain May said, "let's take it off," with first officer Loeffler replying, "can't control this thing Ron." The aircraft became airborne at down the runway. 1–2 seconds after take off, the stick-shaker activated, warning the flight crew that the aircraft was in danger of stalling. The aircraft pitched 60–90 degrees nose-up, rising only feet above the ground. The aircraft then rolled 20 degrees to the right, then sharply to the left, and stalled in a nose-down position. The aircraft crashed into the ground at 16:05:52. The aircraft exploded and burst into flames on impact, killing the crew.

Investigation

The National Transportation Safety Board investigated the crash. The accident was labeled as "nonsurvivable." While examining the wreckage, investigators discovered a foreign object lodged in between the right elevator and the right horizontal stabilizer. The NTSB determined that this jammed the elevator and caused the loss of pitch control, but could not determine how the object got lodged in between the two surfaces, though one scenario stated that the object was blown in by wake turbulence from the aircraft that took off before Flight 863.
The NTSB published its final report on August 18, 1971, with the "probable cause" section stating:

The Board determines that the probable cause of this accident was a loss of pitch control caused by the entrapment of a point, asphalt-covered object between the leading edge of the right elevator and the right horizontal spar web access door in the aft part of the stabilizer. The restriction to elevator movement, caused by a highly unusual and unknown condition, was not detected by the crew in time to reject the takeoff successfully. However, an apparent lack of crew responsiveness to a highly unusual emergency situation, coupled with the captain's failure to monitor adequately the takeoff, contributed to the failure to reject the takeoff.

Aftermath

After the accident, the Federal Aviation Administration instituted new minimums between aircraft in line-up for take-off.