Paks Nuclear Power Plant
The Paks Nuclear Power Plant, located from the small town of Paks, central Hungary, is the first and only operating nuclear power station in Hungary. In 2019, its four reactors produced more than 50% of Hungary's electricity production.
Technical parameters
is the Soviet designation for a pressurized water reactor. The number following VVER, in this case 440, represents the power output of the original design. The VVER-440 Model V213 was a product of the first uniform safety requirements drawn up by the Soviet designers. This model includes added emergency core cooling and auxiliary feedwater systems as well as upgraded accident localization systems.Each reactor contains 42 tons of lightly enriched uranium dioxide fuel. Fuel takes on average three years to be used in the reactors; after this the fuel rods are stored for five years in an adjacent cooling pond before being removed from the site for permanent disposal.
The power plant is nearly 100% owned by state-owned power wholesaler Magyar Villamos Művek. A few shares are held by local municipalities, while a voting preference or "golden" share is held by the Hungarian government.
One brand-new Reactor pressure vessel was bought from Poland after the Żarnowiec Nuclear Power Plant project was abandoned in 1990.
Lifetime extension
In 2000, the Paks Nuclear Power Plant commissioned a feasibility study which concluded that the plant may remain in operation for another 20 years beyond the original 30-year design lifetime. The study was updated in 2005 with similar conclusions.In November 2005, Hungary's Parliament passed a resolution with overwhelming bipartisan majority to support the lifetime extension.
The feasibility study concluded that the non-replaceable parts are in sufficient condition to remain in operation for another 20 years while a minority of replaceable parts needed replacement or refurbishment.
The power generator made repeated surveys of public opinion on the lifetime extension and concluded that support for the decision hovered near 70%.
Following the Fukushima I nuclear accidents in March 2011, Hungary's government said it would conduct a stress test on the Paks Nuclear Power Plant to assess safety, but it would not abandon plans for lifetime extension and it would also go ahead with plans for its expansion.
Unit 1 was granted a license-extension to 2032 in 2012, unit 2 to 2034 in 2014, and unit 3 to 2036 in 2016. Unit 4 got its license extended till 2037 in 2017.
The nine Ganz power generators will be serviced by Alstom one per year between 2013 and 2021.
Power uprating
Thanks to optimizations, modernization and fuel upgrades, it was possible to safely increase the output power of the Unit 4 reactor to 500 MWe in 2006, followed by Unit 1 in 2007. With upgrades to the remaining two units the plant's power generation reached 2000 MWe in 2009.New nuclear units
On 30 March 2009 the National Assembly of Hungary gave its principal consent by votes 330 for, 6 against and 10 abstentions to the preparation works of the possible new units. On 26 February 2010 the owner state company MVM Group decided the expansion with about 2000 billion Hungarian Forints price.On 18 June 2012 the Hungarian government ranked Paks expansion as a "high priority project of the national economy", in this context established a committee for preparation of the factual steps. The Nuclear Power Governmental Committee is headed by Viktor Orbán and has two members; Mihály Varga and Zsuzsanna Németh. As of 2016, Hungary is said to import 30% of its electricity.
According to the agreement signed by Zsuzsanna Németh and Sergey Kiriyenko on 14 January 2014 Paks Nuclear Power Plant will be expanded by the Russian state company Rosatom. Eighty percent of the project's cost will be financed with a 10 billion Euro credit line from Russia. Subject to European Commission approval, construction of two VVER-1200 reactors was planned to start in 2019. On 6 March 2017, the European Commission announced its approval. János Süli, former CEO of the nuclear power station, was appointed Minister without Portfolio in the Third Orbán Government in May 2017, responsible for the planning, construction and commissioning of the two new blocks at Paks Nuclear Power Plant.
On 20 June 2019 the Paks II. Zrt. reported on their website that the preparation of the construction site has started including more than 80 service buildings.
Reactor data
Incidents
Major incidents (INES >0)
2003 incident (INES 3)
An INES level 3 event occurred on 10 April 2003 at the Unit 2 reactor. The incident occurred in the fuel rod cleaning system located under of water in a cleaning tank next to the spent fuel cooling pond, located adjacent to the reactor in the reactor hall. The reactor had been shut down for its annual refueling and maintenance period on 28 March and its fuel elements removed.The cleaning system had been installed to remove dirt and corrosion from fuel elements and control rods during shutdown, as there had previously been problems with magnetite corrosion products from the steam generators being deposited on the fuel elements which affected the flow of coolant. The sixth set of thirty partially spent elements were in the tank having been cleaned, the cleaning having finished at 16:00. At 21:50, radiation alarms mounted on the cleaning system detected a sudden increase in the amount of krypton-85. The suspicion was that one of the fuel rod assemblies was leaking. At 22:30, the reactor hall was evacuated because of elevated radiation levels both there and in the ventilation stack.
At 02:15 the following morning, the hydraulic lock of the cleaning vessel lid was released, and immediately the dose rate increased significantly around the spent fuel pond and the pool containing the cleaning machine, and the water level dropped for a short time, by about. Water samples from the pond showed contamination due to damaged fuel rods. The lid on the cleaning machine was winched up at 04:20, but one of the three lifting cables attached to it broke; and it was not finally removed until 16 April.
The incident was initially given an INES rating of 2. However a video examination of the damaged fuel elements following the successful removal of the lid caused the rating to be raised to 3. This revealed that cladding on the majority of the 30 fuel elements had been broken, with radioactive spent uranium fuel pellets spilling from the elements into the bottom of the cleaning tank. Apart from the release of radioactive material, a concern was that the accumulation of a compact mass of fuel pellets could lead to a criticality accident, as the pellets were in a tank of neutron moderating water. Water containing neutron absorbing boric acid was added into the tank to raise its concentration to 16 g/kg to prevent this. Ammonia and hydrazine were also added to the water to help with the removal of radioactive iodine-131.
An investigation by the Hungarian Atomic Energy Agency concluded that the cause of the incident was inadequate cooling of the fuel elements, which were heated due to the radioactive decay of short-lived fission products. These were kept cool by water circulated by a submerged water pump. However the cooling was inadequate, leading to the damage to some elements through a build-up of steam around them, depriving them of most of their cooling. The investigation proposed that the severe damage probably occurred when the lid was released, causing thermal shock to cladding because of the sudden entry of cool water into the system, and explosive steam production.
One of the interesting results of the investigation was that the Hungarian Atomic Agency had placed too much trust in the technology and knowledge of the French Framatome Company. The agency did not investigate documentation provided by the company deeply enough, missing a fatal design flaw in the Framatome-designed, produced, and operated cleaning equipment.
The discharge of radioactive gases through the stack continued for several days after the incident, although the Hungarian Atomic Energy Agency determined that the radiation levels adjacent to the plant were only about 10% above normal. However, the reactor remained out of service for over a year, finally resuming commercial electricity production in September 2004.
The damaged fuel was completely removed by the end of 2006 and in 2014 transported to Russia for final disposal.