Nuneaton rail crash


The Nuneaton rail crash occurred on 6 June 1975, on the West Coast Main Line just south of Nuneaton railway station in Warwickshire, England.
The train crash happened when the 23:30 sleeper from London Euston to Glasgow derailed after entering a temporary speed restriction at too high a speed. Six people died and 38 were injured. In the subsequent inquiry, the accident was deemed to have been caused by driver error, partially due to the failure of lineside equipment warning of the speed restriction.

The accident

The accident occurred at approximately 01:54, as the train approached Nuneaton station. The train was running over an hour late because of a locomotive failure further south. The train was composed of two Class 86 electric locomotives and 15 carriages, including 12 Mark 1 sleeping cars, two Brake Gangwayed and a Restaurant miniature buffet.
Just south of Nuneaton station, a temporary speed restriction of was in place for a distance of just over a mile because of a track remodelling scheme. The warning board was placed at the standard 'service braking distance' of a mile and a quarter before the restriction. This board should have been illuminated, but was not. The driver claimed that he assumed it meant the restriction had been lifted and did not need to slow the train. It was not until he saw the correctly illuminated 'commencement board' at the start of the restriction that he realized it was still in place, but by then it was too late.
Despite an emergency brake application, the train entered the 20 mph restriction at an estimated and derailed on a sharply curved length of temporary track being used during the remodelling scheme. The locomotives became detached from one another; the first continued in a straight line and came to a stop half way through the station between the platforms, and the second veered sideways, striking and then mounting the northbound platform, coming to a rest after colliding with the platform canopy. The coaches behind them derailed and zig-zagged across the tracks causing severe damage to the track and lineside structures. The first two coaches stayed mainly upright, but the next four fell on their sides, badly crushing the third, fourth and fifth coaches. All the fatalities and most of the injuries occurred in these four sleeping cars. Every vehicle on the train was derailed except the last. The inquiry noted that casualties would have been much higher if not for the lightly loaded nature of the train.
Over of track was destroyed along with three lineside electrification gantries, as well as severe damage to an overhead road bridge, numerous items of trackside equipment, and the locomotive of a passing freight train, which was damaged by falling overhead line equipment.
On board the train was the Minister for Agriculture, Fred Peart, who survived the accident with minor injuries.

The Inquiry

The inquiry, conducted by Major C.F. Rose, found the accident to be due to the following causes:
The driver, Mr. J. McKay, was later charged with manslaughter but found not guilty after a trial the following year.
A number of recommendations to prevent a recurrence of the accident were accepted by the British Railways Board, the main one being the installation of temporary Automatic Warning System magnets at speed restriction locations to ensure that drivers were given audible notice of speed restrictions.

Memorial

A plaque commemorating the victims of the crash, as well as the actions of emergency services personnel, was unveiled at Nuneaton station in August 2015.