George Welch (pilot)


George Welch was a World War II flying ace, a Medal of Honor nominee, and an experimental aircraft pilot after the war. Welch is best known for having been one of the few United States Army Air Corps fighter pilots able to get airborne to engage Japanese forces in the attack on Pearl Harbor and for his work as a test pilot. Welch resigned from the United States Army Air Forces as a major in 1944, and became a test pilot for North American Aviation.

Early life

George Welch was born George Lewis Schwartz, but his parents changed his name to avoid the anti-German sentiment that stemmed from World War I. His father was a senior research chemist for Dupont Experimental Test Station at Wilmington, Delaware. He attended St. Andrew's School. He completed three years of a mechanical engineering degree from Purdue University, before joining the Army Air Corps in 1939. While attending Purdue, he was initiated as a brother of Delta Upsilon. USAAC flight training schools that he attended included: Brooks Field, Kelly Field and Randolph Field in San Antonio, Texas, as well as Hamilton Field in Novato, California.

World War II

After receiving his wings and commission in January 1941, Welch was posted to the 47th Pursuit Squadron, 15th Pursuit Group, at Wheeler Field, Oahu, Hawaii in February 1941.
At dawn on December 7, 1941, 2nd Lieutenant Welch and another pilot, 2nd Lieutenant Kenneth M. Taylor, were coming back from a Christmas dinner and dance party at a rooftop hotel in Waikiki, that ended in an all-night poker game. They were still wearing mess dress when the Japanese attacked Pearl Harbor. Welch telephoned the auxiliary Haleiwa Fighter Strip on Oahu's North Shore to have two Curtiss P-40B Tomahawk fighters prepared for takeoff. Taylor immediately drove his Buick at high speed to Haleiwa to join the air battle. While climbing into their P-40s, the crew chiefs informed them that they should disperse their planes. "To hell with that", Welch said.
Taking off with only.30-cal ammunition in the wing guns, Welch claimed two kills of Aichi D3A Val dive bombers over Ewa Mooring Mast Field. The first Japanese aircraft was only damaged and made it back to its carrier, while the second was finished off by Ken Taylor, shortly before he landed at Wheeler Field to get.50-cal ammo for his two cowl guns. On his second sortie, Welch shot down a Val then one Mitsubishi Zero fighter about 5 miles west of Barbers Point.
Both Welch and Taylor were nominated for the Medal of Honor by General Henry H. Arnold, but were awarded the Distinguished Service Cross, the second-highest US Army medal for valor, for their actions.
After Pearl Harbor, Welch returned to the continental United States to give war bond speeches until being assigned to the 36th Fighter Squadron of the 8th Fighter Group in New Guinea. Despite his aerial victories on December 7, 1941, Welch was dissatisfied with flying the poorly performing Bell P-39 Airacobra. When asked by a journalist what aspect of the P-39 he liked, then seven-victory ace George Welch said, "Well, it's got 1200 pounds of Allison armor plate." This was a reference to the center-mounted engine rather than to actual armor plating. When Welch inquired as to when his squadron would receive Lockheed P-38 Lightnings, he was told, "When we run out of P-39s." He repeatedly appealed to be assigned to the 80th Fighter Squadron until he was granted a transfer. Between June 21 and September 2, 1943, flying a P-38H, Welch shot down nine more Japanese aircraft: two Zeros, three Ki-61 Tonys, three Ki-43 Oscars, and one Ki-46 Dinah. Welch flew three combat tours before malaria brought an end to his time in combat.

Mach 1 claim

In the spring of 1944, Welch was approached by North American Aviation to become a company test pilot. With the recommendation of General Arnold, Welch resigned his commission in the United States Army Air Forces and accepted the job; his rank was as a Major in the Air Reserve 13 November 1944 to 1 April 1953. He went on to fly the prototypes of the Navy's North American FJ-1 and later the Army Air Forces' XP-86. North American originally proposed a straight-wing version of the XP-86 and the Army Air Forces accepted this on May 1, 1945. On November 1, North American, with the aid of captured German technology, proposed and was given permission for a major redesign of the XP-86 to a 35-degree, swept-wing configuration. This was new technology and the USA's first high-speed, swept-wing airplane and a significant advance over Republic Aviation's XP-84. Welch was chosen as chief test pilot for the project.
In September 1947, the first of three XP-86 prototypes was moved from North American's Mines Field to the Muroc North Base test facility, the same base at which the Bell X-1 was being tested. The maiden flight of the XP-86 was on October 1, 1947, flown by Welch.
After about a 30-minute flight, Welch lowered the flaps and gear to land. At this point, the nose gear would not extend completely. For 40 minutes, Welch unsuccessfully tried everything to extend the nose gear. When he reached a low-fuel state, he elected to land on Muroc Lake Bed without a fully extended nose gear. Upon touchdown, in a nose-high attitude, Welch cut the engine, and as the XP-86 slowed, the nose gear snapped down and locked. The aircraft was undamaged.
Secretary of the Air Force Stuart Symington had instructed North American that they were not, under any circumstances, to break the sound barrier before the X-1 achieved this milestone. He could exercise his authority in this regard because both the XP-86 and X-1 were Air Force programs. Welch's only complaints about the aircraft was the J35 engine lacked power and the rate of climb was only a disappointing per minute. North American, however, had already contracted with General Electric for more powerful J47 engines for the production P-86As.
In his book Aces Wild: The Race for Mach 1, fellow North American test pilot Al Blackburn speculates that Welch may have broken the sound barrier 2 weeks before Chuck Yeager in an early flight of the XP-86 prototype. Welch himself never made that claim. Blackburn based his contention on interviews of eyewitnesses, former North American employees, and access to contemporary historical accounts. Robert Kempel, author of The Race For Mach 1 contradicts the claim, contending for Welch's aircraft to break the sound barrier with an underpowered engine was impossible. He notes that the XP-86 airframe was capable of transonic flight, but the interim low-power J35-C-3 limited its performance. The late Bob Hoover, chase pilot for Welch and Yeager, had also disputed the Welch story, stating that Welch was not flying that day because his plane was being repaired. The highest Mach number reached by Welch in 1947, as indicated by official flight test records, was about 0.93, in a maximum power dive from with the engine at 100.8% Military RPM. North American conducted this test, their "High Mach Number Investigation", on November 13. The USAF verified all North American results and this test Mach number in their own Phase II tests conducted in December 1947.
By the end of 1947, the XP-86 had logged 29 hours and 23 minutes of flight test time, most flown by Welch. On October 14, 1947, Captain Charles Yeager exceeded Mach 1 in the Bell X-1. The claim of the XP-86 passing Mach 1, with Welch at the controls, was not made until April 26, 1948, five and a half months after the X-1 supersonic flight. Blackburn, however, maintains that a record on the Muroc radar theodolite, of the two flights Welch made on November 13, 1947, indicated supersonic flights, as well, noting 20 minutes before the X-1 broke the record, a sonic boom was heard over the desert, centered on the Happy Bottom Riding Club, dude ranch restaurant and hotel operated by Pancho Barnes.

Later career and death

Welch went on to work as chief test pilot, engineer, and instructor with North American Aviation during the Korean War, where he reportedly downed several enemy MiG-15 Fagots while "supervising" his students. However, Welch's kills were in disobedience of direct orders for him to not engage, and credits for the kills were thus distributed among his students.
After the war, Welch returned to flight testing; this time in the F-100 Super Sabre, with Yeager flying the chase plane. Welch became the first man to break the sound barrier in level flight with this type of aircraft on May 25, 1953. However, stability problems were encountered in the flight test program, and on Columbus Day, October 12, 1954, Welch's F-100A-1-NA Super Sabre, AF Ser. No. 52-5764, disintegrated during a 7-G pullout at Mach 1.55 from 45,000 ft and crashed in Rosamond Lake in the Mojave Desert about 45 miles north of Los Angeles. When he was found, Welch was still in the ejection seat, critically injured. He was evacuated by helicopter, but was pronounced dead on arrival at the United States Air Force Plant 42 hospital. He is buried in Arlington National Cemetery.
In the 1970 film Tora! Tora! Tora!, Welch was portrayed by actor Rick Cooper.

Decorations

His decorations include: